Saga of the Paradise Trophy Trail |
As you might remember my friend Alan Fraser and I traveled to Paradise California to buy him a Triumph Trophy Trail just as winter set in. It seems bad luck would not stop at the weather. Both Alan and I got colds immediately on returning but we thought we got an OK bike in the deal. I started looking the bike over to see what needed to be done to get the reliability up to my standards, as Alan had asked me to do. Initially between us we decided that it needed a Boyer Ignition with a new dual spark plug lead coil, and a modern rectifier/regulator. Closer visual inspection showed the need of a new rear sprocket, and new cables (the installed ones end fittings did not fit the levers correctly). And for reliability we decided to do away with the original carb and replace it with a new correct Amal as old Amal’s slides tend to stick at full throttle due to worn slides and distorted bodies (from over tightening the hold down bolts). So Alan went away and I started on it. I removed the rear wheel only to find that the installed Yamaha wheel had metric bearings while the axle was english sized, which made for a loose fit of about 0.050 inches. I knocked out the bearings and the internal spacer. I then made a new internal spacer with shoulders on each end onto which the bearings sat and with a hole drilled to the english sized axle. Problem sloved! But what wheel was this that was provided: a 1974 Yamaha, so said the previous owner. But which model. After contacting Sprocket Specialist with all the dimensions we got a sprocket for a 1974 MX250 that fit perfectly. But the counter shaft sprocket was worn out too and that was behind the clutch. So off came the primary cover. The previous owner apparently didn’t see the need for a primary chain tensioner (or a clamp to hold the alternator wiring out of the way of the primary chain) so it was not in there. After removing the clutch and the counter shaft sprocket door there was the sprocket. But wait, it looked funny. The sprocket had hooked teeth and has been ground so as to be able to run 520 chain instead of the stock 530 chain. You see the Yamaha wheel’s sprocket is set up to run 520 chain. But why would a person pay someone to grind down a worn out sprocket? In fact you can run a mix of 520 and 530 sprockets using 530 chain without a problem. We used to do it all the time years ago. So in went a new 20 tooth sprocket (unground) to go with the 51 tooth rear. That will give the bike about 96 MPH top speed which is a close match to my TR5T’s 99 MPH. Through trial and error others have found that the gearing on my TR5T is nearly ideal for dual sport riding. With the new sprocket and a new 530 chain the alignment between the front and rear sprocket was checked (by eye) and found to be OK. Amazing, what with a Yamaha rear wheel and a stock Triumph motor in a stock Triumph frame. The front end was said to be off the same Yamaha (?) but when I unloosened the front axle nut the fork leg spronged to a wider dimension leg to leg. What? Apparently the front end is not a matched set and the wheel is not centered when the brake backing plate is seated against the fork leg. Further investigation showed that the wheel and the extra set of legs provided with the bike by the previous owner were a set. The wheel was never meant to be used with the installed fork legs. In fact disassembly of the front end revealed 35mm fork legs installed in 36mm holes in the triple clamps. The adaption was done with crude sheet metal shims. Not good! So we decided to use the correct 36mm legs supposedly from a Yamaha TT500. Once the correct legs were installed the backing plate fit perfectly. The provided extra axle [modified from some other bike(?)] fit fine after a short spacer was installed on the other side of the wheel (other side from the brake baking plate). It was necessary to push the fork legs well above the top surface of the upper triple clamp to get the bike to ride low enough. Fender clearance (between the top of the tire and the bottom of the fender) was minimise. Of course, the oil was changed in the fork legs before installation and was set six inches from the top of the fork tube with the springs out and the tubes completely collapsed. With the TT500 front end we ended up with 8 inches of fork travel. Now to get ready for a new electrical system the components, the master ON/OFF switch, the rectifier/regulator (Boyer Power Box), the dual spark plug lead coil, and the Boyer Analog Electronic Ignition module, were mounted on a triangular sheet metal plate and hung vertically from the two bolts that in stock form were used to hang the battery box and air cleaner box. That plate went on the right side of the main tube while a much smaller plate, which had the 2.2 amp hour gel cell battery tie wrapped to it, went on the other side. Neat! The lighting was handled by a switch mounted on a sheet metal “dash panel” that used the front two handle bar hold down bolts for support. That same dash panel was used to mount a bicycle speedometer/odometer. A new old stock accessory chrome head lamp (the original plastic one was held together internally with duct tape) with high beam indicator was wired into the lighting switch which had a center off, left for high beam and right for low beam. That same switch also provided power to the rear tail light but only when low or high beams (lights on) was selected. The rest of the wiring was pretty straight forward with a hidden toggle master ON/OFF switch on the electrical components plate. The Boyer trigger wires were routed on the opposite side of the bike from the rest of the wiring to reduce electromagnetic interferrence (EMI) that might cause false ignition triggering. Each circuit carried its own ground from a central ground stud on the electrical components plate that had good conductivity to the frame itself. The latest Boyer instructions revealed that a normal grounding kill button can be used if the system is wired Negative ground (which it was) when that kill button is connected to the Boyer module’s “coil” output. The battery was fused and the brake light was wired so that, whenever the bike is “ON”, the brake light circuit, which includes a switch connected to the rear brake pedal, is operational. Now for the carb. While the carb supplied was the correct 928, disassembly revealed a 330 main jet with other components as per the Triumph parts book. Since the correct main jet is a 180, I think the bike was jetted a bit rich on the top. Funny it ran OK in the mid range. Actually that is to be expected because the main doesn’t come into play until the last 1/4 throttle. The new carb was installed without a problem but being careful to not over tighten the hold down nuts to avoid carb body distortion. The supplied K&N filter was deemed too laborious to clean, requiring overnight to dry out after cleaning and very special K&N filter oil. So a universal (ATV) foam style filter was clamped directly to the carb mouth, which had been modified with a screw on ring that gives a flat surface on to which to clamp. While the installed exhaust system looked OK the oil could not be changed without its’ removal. Not acceptable since the way to make a Brit bike survive is to change the oil frequently. So it was decided to have a new stainless system made up by our local Hesperia welder, Mark McDade. The system was a two into one joining under the center of the engine and exiting as a single larger diameter pipe under the swinging arm, sweeping upward on the bikes right side. As always the fit and finish were exactly as we requested and it looked great to boot with it’s shorty muffler and SuperTrap end plate and baffles. The SuperTrap components make it forest service spark arrestor legal, as it clearly states on the end cap for all to see (including the forest ranger). Through addition and deletion of baffle plates, the noise and power can be tuned. Unfortunately, more noise equals more power and vice versa, but at least you have options. Twelve baffles was selected as a starting point. At completion Alan took the bike for a little ride around his 10 acre property and seemed very pleased. The bike looks good, seems to run well, has no major oil leaks, everything seems to work as it is suppose to work, and above all has that neat twin four stoke sound, not to loud and not too muted. What is to be learned from all of this? No matter how good the bike looks the build quality is no better than the guy building it makes it. My experience is that all these old Brit bikes have been worked on by idiots. For me the only way to do it is to buy a complete, near basket case and tear it down to the last nut and bolt. Paint everything real nice and replace or fix every working bearing, seal, or worn/broken item. Kind of like building it from the ground up. That is the way to be totally confident of the end product’s durability and reliability. Actually we got an OK bike, put about another $1000 into it (assuming we don’t have to do the engine later), and ended up with a good utilitarian bike-not like new but probably reliable and relatively durable. Too bad that most of our time was spent fixing others poor workmanship. It was still a bargain for Alan Fraser compared to my TR5T (perhaps about half, but no engine work was done to Alan’s bike). I would like to thank my good friend, Keith Moore at Moore’s Cycle Center in Anaheim for providing the vast majority of the parts used here, in an extremely timely manner and with his forever helping advice. |