Rickman Chronicles |
Why would a paid-up BSA Owners Club member, who owns an A65 and a B44 want to build and own a Triumph powered Rickman Mettisse? Well, because in the sixties he raced a TR6SC Triumph in the desert, converted it to a Rickman framed version, and later in the seventies bought a Micro Metisse (Hodaka powered) for his "daughter" which he restored. Never mind that she couldn't fit it for about two years. After several years of attending Vintage Motocross races and lusting after any Rickman that would appear, I finally decided to own a Rickman. Restoring one might do but the chances that an old Rickman might have been heavily raced and consequently might have a bent frame seemed high. Or the oil-in-the-frame "tank" might have been contaminated by a blown engine with pieces lurking inside just waiting to get out to damage a newly rebuilt motor just installed. My son convinced me that the prudent thing to do is to build my own from a frame kit and a freshly rebuilt motor using forks and wheels from the used market. This is easy as the frame is still manufactured today in England by a Rickman Brothers approved source. I suspect that the Rickmans provided that company, MRD, with the jigs and all technical data required. The first concern developed as I decided which should come first, the chicken or the egg? The major components were the motor and the frame. An apparent shortage of "ball bearing" Triumph 500 Unit Twin engines seemed that this item was key. I had chosen the 500 verses the 650 because the 500 is inherently lighter. My 650 Rickman weighted in at 325 lbs. The 500 version was reported to weigh 260 lbs. I found this weight to be suspect but the completed bike, if I had chosen to do away with the Lucas alternator and used an after-market electronic magneto installed in the points cover, would have indeed made this weight. My bike weighs about 270 lbs full of gas and oil using the Lucas alternator. Earlier Triumph Unit 500 Twins used the cursed plain bearing on the timing side while the later motors used a ball bearing instead. I found a 1970 ball bearing motor that looked rough but from previous experience I knew that with the right chemicals and some judicious glass bead blasting it would come out looking OK. The motor rebuild became the first project. I did all that I was able to do myself but I had to have the valves replaced and valve seats reground by my friend Keith Moore at Moore's Cycle in Anaheim. Keith also had the cylinder rebored for new pistons. Several "problems" surface during the tear down and inspection. Apparently the previous owner analyzed an engine noise that occurred at the rate of engine rotation to be a primary problem. He had replaced the primary chain, the clutch plates, and the chain tensioner rubbing block. The real problem was that the roller bearing on the primary end of the crank had developed a split on the outer race's circumference and a tang was protruding and dragging on the cheek of the crank. With the engine apart it was no problem to replace and no damage had been done to other components. The new primary components replaced by the previous owner were well appreciated. The transmission gear selector plate showed signs that the track had been over ridden with resultant damage to the plate. This turned out to be a problem as Keith Moore couldn't find one through his sources. Several inquiries on the Internet got me a new one (NOS) from a Vintage dealer in Iowa, Baxters. Most all other components showed normal wear and didn't require replacement except the rockers and their shafts which were replaced with new parts. The motor went back together without a hitch except that long storage without plugs had rusted the bore to the point that even a rebore did not completely remove all traces of rust erosion. Both the boring company and Keith Moore said to run it as the damage to the bore was minimal and acceptable. I then went to Matt Hilgenberg's Speed and Sport in Long Beach and ordered the frame kit. The frame kit includes the frame, the swinging arm, the seat, and all the fiberglass components including the gas tank, the seat base, side panels, front fender, tail piece and the airbox. Included also are key nuts and bolts and a set of chain adjusters (the adjustment is done with cam plates at the swinging arm). Matt also had used hubs from the Montesa version of the Rickman and a set of used Betor forks. The hubs required bead blasting to clean up as did the backing plates. Matt had also provided a set of good brake shoes to go around. The rear wheel backing plate had to be modified to fit on the left side of the swinging arm as the plate was setup for a right hand chain motor. The hubs required the bearings to be changed and new bearing spacers made up on my trusty Smithy Lathe/Mill. The rear axle size of the new frame was larger than the hubs and backing plate would accommodated so the bearing spacer and plate had to be modified accordingly. The used Betor forks were disassembled and inspected. Matt Hilgenberg suggested adding a spacer under the dampening rods to increase the travel to the 7 inch Vintage Motocross limit. The fork legs were cleaned and polished externally but only enough to take off the old patina. That means deep scars were just polished over leaving a bit of character to them. New seals and oil completed the fork leg rebuilds. The triple crowns were bead blasted on the underside and polished on the top surfaces. The top one was modified on my Smithy (mill) to allow clearances around the frame headstock for the handlebar mounting bolts. Handlebar mounts were required so I machined some up using two pieces of one-inch aluminum bar stock for each mount. The two pieces were drilled to match the mounting holes in the top crown, bolted together and bored for the bars at 7/8 inches. The top part or the handlebar mount was milled so that it would act as a clamp on one side. The edges were broken with the mill to give a billet look, which of course they really were. The lower crown had its underside machined such that additional fender clearance was provided. The fender supplied with the Mark III Rickman needs extra clearance when the forks bottom out on those big hit jumps. All fork nuts and bolts were replaced with stainless hardware and the stem was replaced from one off a Bultaco that Matt provided. When the frame kit arrived in less than six weeks from order I was amazed. The build process hadn't started until I ordered it and it was built, shipped, and got through customs in six weeks! The quality was every bit as good as I remembered it from my first Rickman in 1967. The first task was to install the tapered roller bearings for the forks. Matt Hilgenberg also provided these. The forks were fitted along with the hubs in order to determine the amount of offset to the rim for lacing. The rear was problematical in that the rim could not be centered in the frame as there would then not be enough clearance for the chain run. The rear wheel had to be offset 3/16 inches from center for chain clearance as per Matt Hilgenberg's suggestion. Of course I calculated the offsets, laced the rims onto the hubs and fitted tires only to find out that everything hit everything else! On the rear I had used the wrong reference point on the hub when lacing it resulting in a 7/16 inch error. I was able to fix the error and more accurately position the rear wheel, but I had to demount/mount the tire. Oh well, so much for science. The front wheel was off just 1/8 inch, but the tire I had selected had knobs that protruded so much that even after perfectly centering the wheel the side knobs rubbed on the inside of the narrow fender. Oh well, razor blades do wonders for excessively protruding knobs! I had never realized how much tires had changed their profiles in the last 30 years. I next added the engine to the frame and was pleased to find that the chain sprockets lined up correctly. The fiberglass components were installed, making certain that all were well supported and not in any sort of a bind that could eventually cause cracking. Many spacers were made as well as a spigot to adapt the carb to the airbox via a rubber hose. The aluminum shavings were building up from all the manufacturing going on. The spigot alone started out as a 3 inch diameter by 2 inch long solid piece of aluminum with about 80% being machined off. The electrical system required some decisions. I could do away with the Lucas alternator, both stator and rotor, and go for an electronic magneto or use the Lucas alternator, a Boyer Rectifier/Regulator, two stock 6 volt coils (wired in series as per Boyer instructions), and a Boyer electronic ignition. The Boyer Power Module, as the Rectifier/Regulator is called, supposedly allows battery-less operation without using the huge Lucas battery eliminator capacitor. I chose the alternator over the electronic magneto mostly because the magneto device is as scarce as hen's teeth. I was on a waiting list to get a new one for my A65 for over two years and I never got one! The area just behind the steering head on the frame turned out to be just large enough for the Rectifier/Regulator, the electronic ignition module and the two coils. Only the coils peek down below the tank. All else is hidden from view and the Rectifier/Regulator, which requires cooling, is in the air stream. The rear shocks were a bolt-on affair. I used Progressive Suspension rear shocks that I got from our Vintage Motocross racing friend, Charlie Richardson, at CR Racing in Fallbrook, CA. The exhaust system was manufactured in Long Beach by one of Matt Hilgenberg's suppliers, fitted to the bike by a local Hesperia exhaust system guy and plated by a local Hesperia polisher/plater. The carb was a new Amal Concentric that I got from Keith Moore while the air filters are K&N, ordered directly from them in Riverside. Keith Moore also provided all the Triumph motor parts, brearing shells, bearings, gaskets, seals, o-rings, fiber and copper washers required for renewing the engine. Hoses, wire, nuts and bolts, and miscellaneous hardware I got from my local industrial hardware store here in Hesperia. Cables were custom made by Terrycable here in Hesperia and control levers are Works levers bought at Chaparral. Keith Moore provided the entire electrical system except for the Lucas alternator which came with the motor. Matt Hilgenberg supplied the English manufactured, correct Vintage look handlebars. There were a bunch of details that required fitting, or making of spacers, or other unique pieces. To list a few: the rear brake rod and fittings, electrical system mounting brackets, wheel spacers, head steadies, brake stay, and on and on. I could not have built this bike without my Smithy Lathe/Mill, my Harbor Freight Bead Blasting cabinet, and their solvent tank, my drill press, taps, dies, hand drill, hand tools in Metric, Whitworth and American, and all the other tools that I have acquired over the past 40 years. I currently have the best setup shop I have ever had and I do appreciate that fact. For me this was about a project, not just owning a Rickman. The exercise of building the bike is what it was about for me. At the initiation of the project I was offered a recently finished Rickman at a really good price (meaning less than what it cost for me to build mine), but that would not have done the job of providing a bike project, just a bike. If you want a Rickman to have one I suggest you buy a used one. If you want a project that results in a really beautiful 1960 style brand new motocross racer, do like I did and build a "new" Rickman. |